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1973 MGB-GT One Man's Junk... A rust-free low-mileage, one-owner British sports car with 68K original miles gets discovered on a trip to the salvage yard! SOLD 09/08/07 |
NEW SPARE PARTS INVENTORY
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| December 27, 2006 - The MGB-GT got her first night out in a VERY long time. She's been sitting most of the past year, but everything is up and working great. So I decided to go to a local MG Club event tonight. We had dinner at a cafe and then toured a holiday light display. I took her there on the Interstate and the light display required about a half hour of idling along in first gear. No issues, no worries. The new steering wheel really gives her a nicer feel. I need to start driving her! |
| November 27, 2006 - The poor MGB-GT has been sitting in my neighbor's garage for the past few months. Amazingly, she fired right up today. Even more amazing, the brakes are fine! I can't figure how that could be - perhaps there was an air bubble, or it could be that I forgot how the GT's brakes are supposed to feel last time I drove it. Disc brake cars don't have the same 'rock' pedal that drum brake cars have, especially manual disc brake cars. They felt and worked fine today - I drove it around the neighborhood, then out on the Interstate. Smooth and strong, no hiccups. All the electrics are working, and the battery seemed to be fully charged. Mike hasn't been ready for the car yet, but it's looking like we'll get over to his shop soon for the strip and paint. |
| June 26, 2006 - Looks like Proper MG has closed up shop and didn't bother to tell anyone. When I called them to check on my refund more than a week after canceling the order, there was no answer. And no reply to multiple eMails. The web site is still up, but no one answers the phone day or night. I have gotten eMails from other victims who ordered parts months ago and have yet to get parts or money back. Happily, I went to my credit union two days before the 60-day grace period on making complaints expired - I filled out the papers, and had the fund back in my account two days later. On the plus side, I ordered a new master cylinder from B-Hive instead, and got it within 3 days! Very nice folks to deal with, and a good reputation. Now, I need to get the new master cylinder on and get her over to Mike's for the stripping. |
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June 1, 2006 - Hard to believe it has been more than a year and a half since my last update! Sadly, not much has happened with the car. The rebuilt brake master cylinder went bad, so I ordered a new one from Proper MG back in April - and found out today it hasn't even shipped yet! I cancelled the order and will reorder from someplace else. The car still starts right up and everything works. The paint job has been on hold waiting for Mike's schedule to open up. However, I wanted to do SOMETHING on the car, so tonight I installed a new Mountey wood steering wheel I got on eBay. Even got the horn button working! And as an even bigger, better, and scarier option, I have an NOS Webasto Sunroof from Belgium to install when I get ready for the paint job! Can I make that great big hole...? |
| September 25, 2004 - Haven't had time to do much on the GT this summer. I took it over to Mike Muscarella, my painter, back in June to find out what I need to do to get her prepped for new paint. We are going to take her down to bare metal. He marked all the dings and dents (very few considering). The left front tire was going down on me, but I was busy trying to get the 78 MGB sold. Now, with everything else done, I can finally start on the GT again. I got the tire fixed (a nail) and put on a new Monza exhaust system today that I got on Ebay back in July. Sounds great! |
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April 21, 2004 - Finally
got the front shock conversion kit installed tonight. Actually a very
simple job requiring only a few tools. The kit, which I bought on
eBay, retains the original lever-action shocks upper A-arms and adds
tube-type shocks using heavy brackets. The only modification required
is a slight bend to the brake hose mounting tab - about a half-inch is
enough - to clear the shock tube body. The difference is tremendous! Tools required were a hydraulic jack, jack stands, 9/16 and 1/2 wrenches and sockets, a hammer, and a medium Phillips screwdriver. |
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1. Raise front end and support
with jack stands. 2. Remove road wheels. 3. Use hammer to bend brake hose mount back about a 1/2 inch. 4. Remove outer lever shock mounting bolts. 5. Position top shock conversion mount over lever shock mounting holes and secure with long bolts provided. 6. Jack up lower A-arm to relieve tension. 7. Remove two 1/2-inch bolts that secure bottom spring plate to rear A-arm one at a time, replacing with longer bolts provided. Use Phillips screwdriver to center holes as required. 8. Position bottom shock conversion bracket on lower A-arm and secure with bolts. 9. Install road wheels and lower car. You're done! |
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| April 12, 2004 - Got the brake master cylinder installed - took a bit of maneuvering. Whoever did the clutch master was terribly sloppy - only one bolt held the master in, and one bolt held the brake cover on. Naturally the brake light switch broke, but I had another one in the garage. Also got the new grille guard cleaned up and mounted - looks quite nice! | ![]() |
| April 6, 2004 - Things have been rather wild the past two months. Travel to England, Florida, Pennsylvania, and North Carolina has kept me out of the garage. However, I've managed a few things on the GT. Bought a nice grille guard off of eBay, as well as tube shock conversion kits for the front and rear. The brake master cylinder started to go out, and I had to stop driving it. I have rebuilt a master cylinder and have been working to get it installed. Easier said than done, as usual. I'm better than half done now, and hoping to get the rest of the parts installed this weekend. |
| February 5, 2004 - More annoying electrical problems cropped up a couple of weeks ago - the blower fan quit working, along with the wipers. I checked the in-line fuse and it was good, so I have been tracing the wiring. Replaced some bad connectors, but still had no luck. I kept coming back to the fuse. Today, the computer network went out at the office, so I came home to take advantage of sunny weather. This time I tracked all of the connected wires, and ended up back at the %$#@! fuse. It had always tested good before, but this time, I checked it in the fuse holder. The test light flickered as I moved it. At an angle, the fuse showed good. Straight-in, there was no power. Turned out a plastic shaving from the case had fallen inside the fuse holder and was keeping the fuse from making contact. When I was testing the fuse, it would tilt and make contact! I dug it out with a probe and needle-nose pliers, and everything is working again! Oh - the guy who I thought was going to buy the MGB-GT out from under me at the junkyard? He saw me pulling in to a local store this past weekend and came over to talk. A very nice fellow, as it turns out. He was pleased with what I have done to the car, and glad that someone who could fix it up had bought it. |
| January 15, 2004 - The car developed a nasty habit of dieing at unpredictable times - the tach zeroed out and the car quit as if I had turned off the switch. Playing with the coil and electronic ignition module wires fixed it right away - after buying a new coil, I finally decided that the wires of the old Piranha ignition have started to break down. I redid the original point-type distributor and put it in tonight. So far, no problem with quitting, and the car has better pickup. Lots of other things done - the right front caliper's inner piston was frozen, and dusting the wheel pretty bad. I got new loaded calipers from Advance ($54 each!) and already had hoses. I also have the parts to convert to tube-type shocks in the rear. Put on new polished stainless trim rings, a new grille badge, a Coverlay for the dash. new shift knob, and rerouted the heater hose to the intake manifold preheat setup the way it should be. I have put almost 900 miles on the car since December 24th! |
| January 3, 2004 - The weather wasn't as bad as expected, and I drove the car in to work on December 31 after all. She ran fine with the exception of cold starting - the choke linkage was not advancing the throttle. Also the exhaust was buzzing against a cross-member. I ended up driving the car every day as primary transportation every day since. I have been fixing a lot of the little things - put on the new rear bumper guard rubber caps, replaced the bad C-pillar upholstery panel, removed the old, rusty driving light. And today, I gave her a really good bath and waxed her - made quite a difference. Performance has picked up a lot - the car runs and drives great now. |
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| The front shocks are probably shot - I will try adding fluid. Overall, however, the car is a great driver! Mike (the car paint man) is going to show me the tricks on stripping the paint off chemically, and even offered to let me leave the car in his shop while I do it. She will go back to the original color (Harvest Gold?). Maybe in a few months, she'll have new paint! | |
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December 23, 2003 - OK - so I -didn't- get her to the office. In fact, the car wouldn't start at all. The alternator has apparently been shirking its duty, and the battery was nearly dead. I had to roll her out into the street, as I had rather optimistically put her in the back of the driveway. Amazingly, Advance Auto had a lifetime warranty alternator on the shelf for $65! I cleaned and painted the pulley and fan, and did some other adjustments. It is going to rain tomorrow, and the next few days will be spent at my parent's or traveling to my sister's, so she won't get tested until Saturday. But as always, I am hopeful! |
| December 22, 2003 - I took the car over to Chip's again a couple of days ago, and the car nearly expired on the way home. A quick check proved that the points had closed up! Odd. So I reset them and the car ran great - until I headed off to my parent's yesterday and the car tried to expire again just a mile from the house. Once more, I made it back, but just barely. Then I remembered similar woes car nut friend and co-worker Greg Bradner had suffered with Red Car - his magnificent 1966 Shelby GT 350. The condenser on the car had gone bad - we spent some time remarking how neither of us had ever had one go bad before. Well, guess what? Turns out the points were overheating due to the bad condenser, which melted the plastic base and let them close up. So tonight, I yanked out the distributor completely and replaced it with a Piranha Electronic Ignition setup. I actually had two of them in the garage. That seems to have cured the ignition problems. I also replaced the heater hoses - original and looking ratty. So tomorrow I try again to drive her - this time to the office. |
| December 16, 2003 - The gas tank turned out to be badly rusted and full of dirt and varnish on the inside. Cleaning and lining the old one costs $150 and takes a week or more. A new tank is a better deal at about $200, but it also takes a week or more. With the Packard due in two days now, I have to come up with another solution. Like the gas tank I put up in the rafters a good ten years ago. Funny how desperation can jog your memory. Amazingly enough, it is the exact tank I need for the 1973! The inside is clean and dry, and after sandblasting and paint, it's as good as new! | |
| I got it back in, added gas, and the beast started up with only a little fuss. No more dieing or gasping, and after getting her off the jack and outside, I took her for the first real drive - the 4-mile trek to best friend and fellow MG-oholic's Chip Woolford's home. But the Woolford family was asleep at 9:30 - all the lights were out. The good news here was that the car drove very well - strong brakes, tight suspension and steering, lots of clutch and a tight transmission. The gas gauge is working, as are all the other electrics. The car still stumbles a bit, but this is the first time she's really been driven in ten years. Plus, this is the first time out for the combination of Weber, header, fuel tank, fuel pump, and water pump. It will take some tuning to get it all working together properly. But she's drivable now, and everything looks great! |
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| December 15, 2003 - Had to work part of the weekend, but I still managed to get the GT mostly ready. The front carpet is in, and everything is up and running - except for the engine. Fuel supply issues - I replaced the fuel pump, but the problem remained. A glance at the fuel sending unit at right will clue you in on the problem. The car sat for 10 years in storage, and the old gas left a mess. I pulled the tank out rather easily - so far, not one connection or fastener on the car has been corroded or stuck! Believe it or not, the sending unit cleaned up fine, and when I took it apart, there was no corrosion on the inside. Looks like it will work fine - a new one is only $24, but it takes a week to get. I have to get the GT back together before Thursday, when her big older sister (1939 Packard Coupe) comes home after a year and a half of paint and body work! | ![]() |
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December 10, 2003 - Lots of work done on the car - got the parts in from Moss Motors and the Weber back from Chip. I installed the water pump and Weber, plus new hoses and general cleaning all around. Naturally, the new choke cable is the problem - what should be the easiest job is nearly impossible thanks to big hands and tight spaces. I got the new carpet kit in from Too Intense Restoration - if it fits as good as it looks, I have a real winner! Work and other projects are dragging out things, but I am trying to get a lot of little stuff worked out. Replaced the shifter bushing, interior light, and other small stuff. She's drivable as is, but I plan to get the carpet set in and the choke cable on before she leaves the garage. |
| November 30, 2003 - Had a frustrating day today - the car was missing very badly, and then started dumping fuel into the engine. Did a tune-up, and lost all ignition fire. I usually switch over to a Weber and electronic ignition, so I haven't dealt with the dual carb setup or points in a long time. I replaced the fuse block with a new one, and did a more severe rebuild of the carbs, installing new float valves. Still dumping fuel. My best friend Chip looked at the carbs and determined that the main needle valves were damaged by corrosion. I pulled a spare set of carbs from the garage and put them on. Took another look at the points and realized I had connected the ignition and condenser leads wrong. ::duh:: Once that was done, the car fired right up - and up - and up. The carbs are set way too high, but some adjustment got it down to a reasonable level. The engine sounds very strong, no smoke, all gauges and accessories working - even the British Leyland AM-FM radio! I will probably reclaim my spare Weber setup from Chip's MGA - but I gave him the parts he needs to get the original MGA carbs together. Oh, got the exhaust system done yesterday - looks and sounds good. I also did some cleaning and painting of engine stuff. The car will need a water pump and a few small bits, but all-in-all, she is shaping up very nicely. |
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November 26, 2003 - OK, I was a little optimistic. After replacing the coil, I got the car running on Saturday. Barely. The carbs were gunked up inside and the exhaust down pipe was shot, but I was able to drive the car around the block. The brakes came up on their own after I added fluid to the master cylinder. I sandblasted and painted a set of Roistyles and had new tires mounted Wednesday - I put them on tonight, and have new emblems drying on the center caps. I had a nice ANSA exhaust header which I sandblasted and painted tonight. The carbs got a light overhaul last night, and look good. So far, except for the tires, I have everything the car needs already in the garage! |
| November 17, 2003 - Another accidental discovery ends up in my driveway. My best friend Chip was the one who spotted this 1973 MGB-GT in the 'for sale' area as we were leaving U-Wrench-It salvage yard this past Sunday. Now, finding any MG in a junkyard these days is odd - but after careful examination of every nook and cranny, we discovered that this was something never before seen by human eyes - a RUST FREE MGB! |
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Once we got over the shock, we also noticed that the car was undented, and every body panel was as straight as the day it left Abingdon. After checking the interior for signs of Big Foot and the gas tank for the Loch Ness Monster, we went inside to see if this mythological creature really existed. Only to find out that it had just come in and a price wouldn't be assigned until Tuesday. I was given instructions to call after 10 a.m. Chip already has a GT, and is also a responsible father and husband - i.e., his wife would kill him if he brought home another car. So by default, I had clear shot. |
| But only with Chip. Evil,
in the form of other interested parties, had already been lurking around
my MG, and I had no doubts others would be lusting after the little GT.
I called on Tuesday at 10, and again at 10:30 when the boss turned out to be
in a meeting. The price was $750. I offered $650, and we agreed
on $700.
EXCEPT - money talks - the car would not be mine until I was there with the cash. My original plan was to leave early from work and get over to the yard about 4 p.m. However, I had a gut feeling that was a mistake, and packed up at 11:30 for a quick trip home to grab the truck and tow bar and stop by the Credit Union. |
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I walked in the front door of
U-Wrench-It at about 12:30, just as a man was walking out towards the MG
saying "Yeah, I was here Sunday, but I couldn't get the hood open."
The yard owner explained that the guy was going out for a final look.
And since he had come before me, he had dibs.
A filthy, disgusting usurper had come to claim MY car! I had to stand there, money in hand, waiting for the guy to make a thorough inspection. I very carefully avoided the area so he wouldn't know there was a vulture circling. When he finally came back in, I braced myself for disappointment. Only to see him walk right by the counter and off into the yard without saying yeah or nay. The boss shrugged, and said "Sold for $700." The car was mine. The would-be MG thief (at least in my eyes - he probably views me the same way) had gone out to look at another MGB in the yard, probably figuring he could barter if he played it cool. I was hooking up the tow bar when he came back to negotiate. Why so excited about a 31 year-old car from a junkyard? Well, the GT is my favorite body style, and this one hasd a near-perfect body and glass, decent interior, and nice chrome! Plus, I had a feeling about the car - it was in awfully nice shape throughout, and the fluids were up to the level and clean.. |
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| I called the previous owner
that night, using the name on the title. Turns out he bought the car
new, and the 68K miles on the odometer are original. He drove it as
a fun car in good weather only, logging just 64,000 miles by 1994, when he
had the upper end rebuilt. Shortly afterwards (68K miles), he decided
to put it in storage. He lost his storage recently, and decided that
he wasn't interested in working on the car any more. So he went for
the tax write-off and called the Kidney Foundation. Other than
problems due to the long storage (BAD gas, dirt, fading, etc.) the car had
no problems he was aware of! As you can see from the photos above, a wash did wonders for the car. The clutch hydraulics are still full up, and the carbs freed up with one tug. They even had oil in the pots! I drained the old gas out tonight despite moderate rain, and will buy a battery tomorrow. I'll flush the lines and add fresh gas, then see what happens. Odds are good that I'll be driving the car this weekend! |